Control System Integrator Saves
Energy with Advanced Technology
Bernard Pelletier and Vance VanDoren --
1/1/2003
Advanced control techniques can be used to extract additional energy from the by-products
of chemical reactions known as ''off-gases.'' Off-gases produced by chemical, petrochemical,
and metallurgical plants can be reused or sold, depending on the season. Optimizing
off-gas usage has become one way to remain competitive, as energy costs have risen
over the last five years.
The necessary techniques, such as feedforward control, can be programmed into an
existing control system as part of a four-step plan:
- Develop a good understanding of the process and its operation;
- Develop a good understanding of the existing control system;
- Define proper control objectives and manipulated variables; and,
- Apply the right advanced control technique.
And because specialized software packages and instrument purchases are not always
necessary, a very high return on investment is possible.
Adaptation to ''real life''
One example of optimization steps applied to off-gas usage is in an ilmenite reduction
plant operated by QIT-Fer et Titane (Sorel-Tracy, PQ, Canada). Carbon monoxide (CO)
gas is generated as a byproduct of the reduction process in large quantities. It
has a high caloric value and is used as a fuel gas across the whole QIT metallurgical
complex.
Smelting furnaces produce CO gas while rotary kilns, boilers, coal dryers, UGS [define]
plant, and other users consume it. A gas holder between production and consumption
stores the CO to absorb high-frequency disturbances and keep gas pressure constant
in the CO piping network. The gas holder has a movable membrane roof and a residence
time of less than one minute.

This graphic shows the initial plant
arrangement and the original PID control strategy for maintaining CO level in the
gas holder.
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Two flare stacks with control valves are used to burn excess CO production when
the gas holder level reaches its upper limit. Kilns burn both CO from the gas holder
and natural gas at a mixing ratio varying between 0 and 100%. The natural gas allows
the operation of the kiln to be maintained when CO production and levels in the
gas holder are low.
The old control strategy was built with the exclusive objective of maintaining a
tight gas holder level, using two conventional PID controllers in a cascade arrangement.
A master controller regulated the gas holder level while a slave controller regulated
the mixing ratio of the kiln fuel. Output of the level controller was split into
two parts-0% to X% was used to modulate the mixing ratio setpoint while X% to 100%
handled modulation of the flare valves.

Typical CO gas production and consumption
over any 24-hr period caused wide perturbations to the gas holder level.
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Originally, there was no dynamic coordination between the flare valves and the mixing
ratio. As a result, there were times that perturbations to the CO level caused the
control system to burn off excess CO gas and feed natural gas to the kilns at the
same time, This occurred in spite of availability of CO gas. Such unstable periods
typically lasted for just a few minutes, but were costly to QIT, especially as the
price of natural gas increased.
Enter the new strategy
Solving the problem required a new strategy using feedforward control. It was applied
to the QIT-Fer et Titane plant using the four-step plan as follows:
- Understand the process and its operation - CO gas production and consumption vary
considerably over short intervals (see accompanying graph). Unfortunately, this
cannot be changed due to the overall plant production schedule and constraints.
However, CO production and consumption can be measured and analyzed to identify
the process delays caused by the distribution piping. The longer the delay, the
harder it is for the control system to compensate for disturbances. A detailed analysis
of CO gas consumption also revealed that the major and most frequent disturbances
are caused by the UGS plant. Delay between this user and the holder tank is 20 seconds.
The delay between the CO producers and the holder tank is only half that.
- Understand the existing control system - When a disturbance occurred due to variations
in production or consumption, the control system took action too aggressively and
too late because of delays. The holder tank level controller was tuned aggressively
to react quickly to disturbance, causing the manipulated variables to swing. This
in turn caused simultaneous flaring of the CO gas and increase of natural gas flow
to the kilns.
- Define proper control objectives and manipulated variables - The new control strategy
has the same manipulated variables but different objectives. They include maintaining
the gas holder level in a certain range and coordinating flares and the mixing ratio
to prevent flaring when natural gas is being fed to the kiln (and vice versa). In
the old control strategy, tight level control was the only objective. In the new
control strategy, 'smoothness' is included in the controller's objectives to reduce
the manipulated variable swings. An economic objective was also introduced. This
important objective is too often forgotten or not well defined and applied in industrial
applications. The new control system also takes advantage of certain measurements
of CO production and consumption that were being collected for other purposes but
not being used by the old control strategy. No additional instrumentation was required.
This demonstrates the importance of carefully evaluating the controller's information
requirements to avoid unneeded new instrument purchases.
- Apply the right advanced control technique - Feedforward control was chosen as the
most suitable advanced control technique for this application because the disturbances
are measurable, well known, and easily modeled from archived process data. Gains
and time constants of the disturbance model were computed from process data stored
by the existing historian.
Achieving objectives
The new objectives were achieved by introducing three new elements to the control
strategy. These included the addition of feedforward controllers based on a mass
balance calculation (consumption vs. production), dynamic compensation for transport
delays, and the coupling of flare valves and the gas ratio controller to prevent
overlap.

Addition of advanced control strategy
has reduced periods of simultaneous CO gas flaring. Natural gas consumption is down
by 76%, representing sizeable savings in natural gas costs.
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Six feedforward controllers have been implemented to handle two disturbance variables
(CO production and UGS plant consumption), three manipulated variables (two valves
and the mixing ratio), and one controlled variable (the gas holder level). Other
users are not included in the feedforward loop since their CO gas consumption is
fairly stable.
Feedforward controllers provide lead/lag compensation for transport delays based
on process and disturbance models. The feedback loop controlling gas holder level
has been retained in the new control strategy to keep gas level at its setpoint
and to correct for model errors in the feedforward controllers. However, the level
controller's PID parameters are tuned less aggressively since the feedforward controllers
now provide the major correction when a disturbance occurs.
Case for simulation
The new control strategy was initially simulated with Simulink, a Matlab toolbox
from The Mathworks (Natick, MA) to minimize costs and to expedite the schedule.
The simulator was built with simple first-order-plus-delay transfer functions and
was tuned with archived data.
The simulation helped with the design of a better and faster customized solution,
and also facilitated the commissioning. The new control strategy was pre-tuned with
real CO gas consumption and production data imported to the simulator. Special cases,
such as plant shut down, were also simulated to make sure that the advanced control
strategy would be safe.
The strategy was then implemented on QIT's control architecture, a Modicon PLC from
Schneider Electric (North Andover, MA) and human-machine interface by Wonderware
(Irvine, CA) without any additional hardware or software expenditures. The program
was modified using ladder logic language.
Since the commissioning of this advanced control strategy, the periods of simultaneous
CO gas flaring and natural gas usage have been reduced by 76%. This reduction represent
natural gas cost savings of up to C$ 1million (Canadian dollars) per year.
Author Information
Bernard Pelletier is an advanced control engineer for Hatch Associates (Mississauga,
ON, Canada). Vance VanDoren is consulting editor for Control Engineering.
Online Information
For more about Hatch and more than 1,000 other system integrators and automation-engineering
firms, log on to the Automation Integrator Guide at www.controleng.com/integrators .
© 2004 Reed Business Information, a
division of Reed Elsevier Inc. All Rights Reserved.
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